RIP 7bolt
Thread Starter
Douchebaggery!!!
Joined: Dec 2002
Posts: 641
Likes: 0
From: Preferably some place warm.











go to www.roadraceengineering.com they have some info on it. It didn't happen with the 1st gen motors only in the 2g's
Originally Posted by SLO-4G63
go to www.roadraceengineering.com they have some info on it. It didn't happen with the 1st gen motors only in the 2g's
hahahahaa, hybridawd was joking.
Thread Starter
Douchebaggery!!!
Joined: Dec 2002
Posts: 641
Likes: 0
From: Preferably some place warm.











Well after further investigation. The problem was the accessory belt that drove the ac compressor. When it broke it wrapped itself around the main pully and up against the timing cover. So it caused the car to eventually stall. When the car stopped due to the resistance and I tried starting it again that's is when we think all the damage occured. While shineing a flashlight down the number 4 sparkplug well. You can see where one of the valves dropped down and got rammed back into the head and had logged itself in the piston DOH!!. So it looks as though a new motor is in order thinking about trying to find an evo 3 motor since I hear that they are a direct dropin. Plus now since this has happend I picked up a daily driver and am seriouly thinking about turning the GST into a weekend warrior. Oh well just thought I would share the new info with all of yall.
Thread
Thread Starter
Forum
Replies
Last Post






